Testing and "Racing" at Brands

Not a great weekend, no major damage, but generally a bit disheartening in how slow I
was but the car held together with only a few teething problems. Of most concern is it’s lack of straight line speed relative to a much less powerful car (Judy’s) I think it is just too damn heavy and with less power now there is simply nowhere to hide.

As a result I’ve decided to cease developmental effort on this chassis and contemplate building a new lightweight one over the winter. In the mean time I intend to drive this one to death. Plus I need to lose some flab… but that’s obvious

On the plus side, car is smooth and pretty well balanced, the new brakes work and it is not displaying any nasty habits or snap oversteer in fact the only adjustment change I made all weekend was to knock a single click off the front dampers to kill a bit of understeer in Clearways. And my manual alignment was within 20 minutes of arc of being perfect. Plus the RGB paddock is full of great people.

Friday Testing.
I arrived Thursday night, Tim and I had arranged to share a garage so I unloaded and parked the car up in the garage. Tim was already fettling, so I took the opportunity to do a few extra things like stick on the CAM7 stickers. Tim and I got to sleep around 2 am and where up with the lark, or at least with Brands noisy indigenous bird population anyway.

I managed three test sessions on Friday, The first was a 6 lap shakedown, taking it easy and just seeing how things went. Pretty early on it became apparent that the cooling was crap. Even taking it easy oil temps were climbing to 120 and water towards 100. Not good and on reflection there is something seriously wrong here.

However I came in to check it over and see how things were. The only major issues were that the chain had stretched, and the shift lights were not working. So after giving it the once over and a brief stint to cool down, I went out again and gave it some beans. In about 6 laps I managed a 59.59 (front runners are in the 52s) but the coolant went to 120 and the oil to 140. So I decided to do a couple of laps touring round to cool it. but just then they red flagged the session so I had to bring a cooking engine straight in. Of course when you kill the engine the coolant pump stops and it immediately boiled over. Later inspection also showed that the radiator was also weeping a bit from one for the pressure margins where the metal and plastics are crimped together so the pressure had got just a bit too high and things are getting pretty hot.

After mopping the coolant from the garage floor, giving it a couple of hours over lunch to cool down, refilling it and fixing the rad. I thought I’d go out and do 4- 6lap bursts to get some value from the day. Again it over heated badly in the afternoon so I didn’t get to do much, and my data logger failed to record any times either.

On the last session I bought it in and it was sounding like a bucket of bolts and only running on three. Really carp. I thought I’d badly cooked it. However Andy Bates came and looked at it and identified a stick coil that had jumped from the plug… and a couple of missing nuts on the exhaust manifold. Once these were repaired it sounded ok. But I decided not to risk it further.

However I wanted to fix the cooling issue before the race on Sunday so a quick call to Tim Pell indicated that there was a larger radiator that I could fit so I ordered one of these (from a 2Ltr Meastro Turbos Diesel) on the way home and collected the new radiator on Saturday morning. I then spent14 hours on Saturday fitting the new rad, cutting a vent hole in the front bodywork, making the aluminium shrouding to duct the radiator exhaust air out through the hole and fitting an auxiliary electric coolant pump. All in an attempt to get some heat out of the engine. I also refitted the electric coolant pump so that I could keep the cooling system running after shutting down the engine.

Duncan arrived around 5pm and identified an even bigger problem.
The Diff has twisted sideways under drive tension from the chain (this was what was allowing the chain to slacken)and the bolt heads holding the drive sprocket had started chewing into the steel shear plate at the rear, so he spent a few hours making a burly steel support to stop this happening. All in all we finished around 10pm. Essentially the tension under load is pulling the driven sprocket forwards. As the left mounting plate prevents the left mount from moving forward what is actually happening is that the right hand mount is moving backwards and the rear end of the diff moves to the left as the whole thing pivots around the left hand mount.So I need to stop this happening using different tension fittings on the mountings.

On Sunday I was up at 5:30, Dunc arrived at 6 and we reloaded the car on the trailer and set off once again for Brands, hopeful that we had fixed the problems.

I arrived in the paddock to much congratulations for actually making it to a circuit and some gentle ribbing, but it was nicely balanced with some genuine admiration for the neatness of the engine installation and some nice “Welcome Back” hand shakes from the RGB paddock. It was really very very nice to be in the paddock again. In fact sometimes it was hard to get to car to stick the stickers on it because everybody was stopping by for a gawp and a chat :-)

The car passed scrutineering first time, and so it was on to practice. Somehow I arrived early and ended up fourth in the queue. Once the session started my over heating problems seemed to be a bit better, I was running at about 1:05 deg water…. dunno what the oil was as I hadn’t managed to load the updated software from Tim onto the palm on Saturday and it crashed on lap one, driving Round Brands… resetting a plam pilot will definitely put a kink in your times. :-)

So after 6 laps and with the whole field streaming past me (not a good sign) and the coolant running towards 110 again I decided to call it a day and come in.

The qualifying times came in and I was dead last. 59.6 I think, which is 1.1 second down on my fastest time from last year, but then I did have the kwacker.

In between practice and the race we tested the engine and were concerned to see that the secondary injectors were not firing, so we spent a couple of hours chasing down the fault. But it wasn’t a fault, it was a ghost. Everything checked out and eventually when we re tested them by stamping on the throttle rather than winding it up gently they worked fine. So they are not the reason I was slow. I’m slow because I’m slower than a slow thing out for a Sunday stroll pushing his infirm slow granny in a slow thing’s bathchair!

When race time came I was lined up on the grid dead last with Judy in her class C Fury next to me, when the lights went out, she got the jump on me and we were off. At Paddock I briefly thought about diving up the inside but wasn’t really close enough and on the way to Druids passed Gordon G’s stricken car in the gravel on the left. Round Druids and there were two other RGBs spinning into the ARMCO on the left and so unsurprisingly the race was red flagged while they cleared up the carnage. On the restart we made it as far as Clearways on Lap 2 before we found a spinner in the gravel and we had earned ourselves another red flag plus a group bollocking from the Clark and retirement to the end of the meeting. The Observers reports used words like “disgraceful” pretty bad stuff. Apparently people were still banging into each other when the red flags were waving but I was too far back to see it or be involved.

So as the last race of the day we restarted and this time I managed to hang on to Judy for a couple of laps and was actually trying to go up the inside of her at Clearways when I missed the selection from 2nd to 3rd. By the time I had found a cog she was 100 yards up the road and I went down the straight swearing loudly. Difficulty selecting the right gear for Clearways was to be a recurring theme and marred the rest of the day (such as it was) . In fact I suspect in frustration I yanked the lever a bit hard as I seem to have bent it! I hope I haven’t damaged the gearbox selector forks. If not then Mr Honda’s engineering really is bullet proof.

Although I felt I was getting faster in Paddock, Surtees and Mcleans, Druids and Clearways remained crap. Particularly Clearways which is the crucial corner for Brands. After about 8 laps and having been lapped the temps started to climb again so I abandoned it and headed for the paddock. Once there I discovered a stone hole in the nice new radiator that had done precisely 15 laps. :-(

So the take home messages are

  1. It needs an oil cooler, I think the oil is currently heating the coolant through Mr Hondas standard oil\water heat exchanger and for some reason I can’t keep the water cool. Either that or I need a wire basket to cook my chips in the boiling oil.
  2. I’m slow, dog slow…. glacial in fact
  3. The engine seems to be pretty strong in terms of standing up to abuse.
  4. Most of the work this winter seems to be wasted as the power loss certainly isn’t counteracted by the weight loss.
  5. Last year I was plainly using the power of the kwacker on the straights to mask my crap cornering. with less power now there is nowhere to hide.
    Must get better!
    Hmmph
Posted in Cooling, Radiator | Leave a comment

Final Pre Race Setup before Testing

Well the final week before the Test at Brands passed pretty quickly and as usual I never got to do the everything on my to do list. For years I’ve been making lists about the car to make sure I don’t forget stuff and in this respect (as my wife pointed out) I’m like my Mum. We’ve never visited her without finding an old envelope and a pencil on her kitchen counter with a list of things to on it. I guess there are things you learn at your mothers knee that you don’t even realise. On the subject of lists I also learned from Tim that the categorisation that I tend to do for my lists is actually known as a MoSCoW list. Which is Must do (IE critical), Should Do (preferable but not essential), Could do (if enough time) and Would do (in an Ideal world).

Most of the last Saturday before the test was taken up with wheel alignment and general chassis setup. I’d never done this before from scratch and so again following Tim’s advice I gave it a go. Starting with ride height, then wheel camber, then front and rear toe in, then front\rear alignment and finally corner weights.

This whole process took all day and necessitated the construction of a few adhoc tools. One of these was a combined alignment \ride height gauge made out of a piece of angle Ali angle and an up stand. The gauge is actually 83 mm tall so that when I sit in the car the resultant suspension squish drops the car to the regulated 75mm (which is about the best approach when doing it on your own.) On the back of the gauge was a graduated scale which I used to check alignment. Basically I stuck a magnetic laser level on each rear wheel and held the gauge on the front wheel and then adjusted the rear toe control until the pointers hit the same mark on the scale when it was held on the front wheels. Then with the laser on the front wheels and the gauge on the back this gives me fore\aft wheel alignment around the centre line of the chassis. Then when adjusting toe in if you move each side the same amount of turns the alignment should be maintained as you dial in the settings.

I also made a toe in gauge, which is basically a long U of steel so that you can measure the relative distance between the front and rear of each pair of wheels. The method was to position the bolt head on the wheel rim on one side of the car and then use a set of digital calipers to measure through a hole in the steel to the rim on the other side of the car. Zero the digital caliper in that position. If you then move the gauge to the front of the wheels and re measure you can directly read the toe in value off the calipers.

I was aiming for toe in of about 1.5mm at the front and parallel or a very tiny amount of toe in at the rear. It took me all day and by the end of it I was far from certain that I’d got it right. but it seemed ok

So the complete set of alignment settings were

Front ride Height 83mm
Rear Height 95 mm
Front Camber 1 3/4 deg
Rear Camber 3/4 deg
Rear Toe in – parallel
Front Toe in – 1.5mm
Front Dampers 8 Clicks
Rear Dampers 10 Clicks
Tyre pressure 18.5 psi all round

Unfortunately I didn’t have time to do the corner weights, so I still don’t know what the ultimate weight saving is from stepping down to Class B and changing the engine

So after 6 months of gestation it was time to take this new engine, diff and chassis combination to the track and see what it could do.
Posted in Moscow list, toe in | Leave a comment

More progress to report :-)

First up I completed the wiring for the new rainlight that is now required by this year’s regulations, OOOOh look a glowing set of LEDS that look almost identical to the last set of glowing LEDS that were fitted there. You’ll have spotted a pattern that most of my jobs are now the little things that are requried to meet the RGB series regulations. This is a good sign as it means that I am now focusing on the smaller jobs rather than major structural or mechanical components, ERGO I’m getting to the end of this.

Next it was on to that leaky front Calliper. A quick test on Tuesday night indicated that both the left and right calipers were leaking when under heavy pedal pressure. Both from the same place; where the top halves of the caliper are joined by the removable aluminium spacer. If you remember the picture of the handbrake calipers this is where the fluid cross over drillings are located and the two sides are pressure sealed by a rubber O ring. I suspected that the O rings had aged and failed and a call to Hi-Spec confirmed that this can happen. So a couple of rebuild kits were duly ordered and should be here for the weekend. That will mean I need to disassemble the calipers which in turn means I’ll need to bleed the brakes ….again!. Shouldn’t be any bubbles in my fluid. No sir!.

The other job identified last weekend was that the reverse control needed a control lever to get sufficient mechanical advantage. So I’ve quickly fabbed one up out of a strip of ali bar stock. This now makes operation of the reverse very easy. So easy in fact that I was concerned that the system would jump out of drive if knocked by my arm, so I fitted a retaining spring to the diff to hold it in the forward drive position. Of course this does mean that I’ll have to manually hold it in the reverse position to actually go backwards, but this is preferable to false diff neutrals in a race, also it means it should slip in of it’s own accord If I happen to miss the engagement dogs. Also as is my own particular habit I labelled it up clearly because it is slightly counter intuitive (pull back to go forward) but also because I forget stuff!

The other major system ( and the last to be done) that was completed this evening was the handbrake, having finally got calipers to fit I needed to connect them to the handbrake lever. This entailed welding a couple of mounting plates in the rear frame (next time I’ll get these made up as part of the laser cut plates). And adjusting the sierra handbrake cable to fit. It took me a couple of attempts to get the routing tight so that the wires didn’t get cooked on the exhaust but in the end we got there. And I now have a working hand brake….. well working good enough to pass scrutineering. :-)

The plates will need painting but this is hardly essential before Brands on the 20th.
Then came another regs job. All chain driven cars must have a chain guard fitted to stop the chain exiting upwards or rearwards if it snaps (and they do). So a few minutes were spent with some Ali angle and I got about 60% of this particular job complete. Other small jobs that got done in the evenings this week included torquing and staking the front hub nuts in place, replacing the DL1 sensor, fitting locknuts to the Diff spacer plates and lockwiring the diff and sump plugs.

The To-Do list now numbers just 22 items totalling about 14 hours in estimates and ranges from essential stuff like Set Toe In, Ride Height and corner weighting (4 hours) to the less vital .. check and adjust pedals for heel toe (10 mins) and fit race numbers (15 mins) and finally to the nice if time category including polishing the beast.
Posted in handbrake cable, rain light, Reverse | Leave a comment

Nearly There!

Well over the last weekend I’ve got an awful lot done, which is good. but pressure of work means that I’ll have to cancel my test at Mallory and test closer to the Brands meeting on the 20th, which is less good, although it does relieve some of the time pressure.

No 1 and most importantly I’ve finally got a complete and working braking system and managed to fit the new 14″ alloys to all four wheels for the first time. The hassle necessary to get the various combinations of calipers, disks, offset, calliper mounts, spacers, 14″ wheels, leaky master cylinders, alloy bells, rotors, suspension bolts heads and brake pads into a combination that allows the car to both move without the brakes\calipers\pads binding and stop properly when you push the middle pedal is simply incomprehensible. Take my advice If you ever….. ever EVER build any sort of racer or kit car choose one that uses standard uprights (the bits that hold the hub,bearings and calipers) and standard caliper mounts. Then you can choose a known, working off the shelf kit where somebody else has invested the necessary blood sweat and tears. If you have to fabricate or sort any of this part of the car out yourself be warned it is a seemingly endless trail of frustration and woe.

The latest in a long stream of issues was that the pad depth on my Mintex 1144 pads was too thick to fit across the new 9mm rotors, what this means is that you a) have to grind slightly one edge of the pad backing pad and b) reduce the thickness of the friction material a bit using a file simply to get the pads to fit over the disks and then to get them both to fit in the caliper slot. And this despite me ordering calipers with a slot specifically tailored for 9-12mm rotors. I chatted to Hi-spec about this and they said “yeah!…. we’re having lots of trouble with the pad manufacturers altering either backing plate designs or pad depth….. file em to fit”.

Bah filing pads every time I need to change them seems like a job I don’t need.

Hmmp, anyway after an inordinate amount of frustrating tomfoolery (which also included me copiously testing my garage floor paint’s immunity to brake fluid) everything was finally fitted and ready for bleeding. Bleeding the system identified a couple of leaking unions (one of which was on a master cylinder which then had to be replaced). But eventually we got there. And I finally have a working brake system. Due to replacing the master cylinders and cleaning the pedal in the last post I probably need to adjust the pedal rest position to allow me to heel and toe properly but compared to getting to this point that should be a doddle.

It was only later that I noticed a slight leak on the front left caliper that I’ll need to investigate next week.

While I spent a “pleasurable” few hours sorting out the brakes Duncan was fitting the exhaust more permanently. Tony Law had done a good job of fitting it, but had failed to account for the fact that the Diff slides backwards when the chain is tensioned. As a result when the Diff was in it’s final position the CV boot rubbed on the exhaust can. The solution was to cut off the existing slip tube which formed the exhaust joint, and add one about 3 inches longer. This allowed the Can to be positioned further back away from the CV joint. With this sorted out he then set about fitting an axillary support to both the can and rear body support frame. By his own admission he wasn’t very pleased with either his welding or the fact that he designed the whole thing “in peel”. Still it is at least sturdy enough for one or two races so I’m not going to worry about it now and as always I’m more than grateful for the help.

Other stuff that got done today or in the last few days included.
Torque the front hub nuts, finalise and tighten the gear linkage, tap and fit the new gear knob that Dave T had made for me, renew rear suspension Nylocks, flush the diff with petrol and fill with new gear oil. Lock wire diff drain plug, change a couple of CV joint boots, fit new brake lights connector and replace the temporary plastice cable ties with nice stainless steel ones. Tighten rear sprocket bolts, bolt check suspension and fit new calipers.

The other major piece of work that got done in the engine bay was to complete and fit the airbox. This required connection of the secondary fuel rail to the main one via a -4 bulkhead fitting and wiring the electrics via a suitable grommet. Plus I needed to make a new cover plate for the rear of the box. I made this out of clear perspex and finally got to discard one of the last vestiges of the fire… the old airbox cover.

So now the engine bay is complete bar one little job (I’m going to re route that fuel hose left on the which looks to be in peril from a flailing chain) I have to say I’m pretty proud of it. It looks neat and tidy and properly designed.

At the end of the day, Duncan got his just desserts and had the honour of driving the beast up and down the drive.

True to form this small test identified another little job, the reverse select T bat does not provide enough mechanical advantage to make selection reverse\forward easy and so this will need a lever fabricating.
Posted in Exhaust pipes | Leave a comment

The long list of Odds and Sods.

You know I can always tell when I’m getting towards the end of a build the engine bay starts to look like it has been visited by the NASA fairies, as I finalise the cable and fuel line routing and fit the shiny silver heat protection sleeving.
I got most of this work done on Sunday, and also did some preparatory work on the running the fuel and electrical lines from the main bank of injectors to those in the airbox in readiness for fitting it to the car.

In addition I fitted the catch tank, and bolted the exhaust headers, tightened up the gear linkage and did a few other bits and bobs jobs.

I’ve also dismantled, lubricated and rebuilt the brake pedal as it had got a bit stiff and recalcitrant about returning to the rest position. I wondered if the master cylinder springs were getting a bit weak and so disassembled the whole lot to clean, strip and check it. Ultimately it turned out to be binding in the pedal pivot point and the MCs were fine. This whole exercise took up a couple of hours and of course I need to re bleed the brakes again.

I’m currently working towards a shake down test at Mallory Park on the 9th May, and the plan is now to complete the build and setup the car over the bank holiday weekend, then go to the test, and then work on the Bus so that I can get it through it’s MOT before I need it to go to Brands on the 20th.

Time will tell :-) . but currently the planets do seem to be aligning for me at long last

Posted in Winter 2008 Rebuild | Leave a comment

It Moves!

The car has today, moved forwards and backwards under it’s own steam. Given that I’ve pretty much completely replaced the engine, transmission, clutch & brakes you can imagine the was a pretty big moment. :-) .
An added advantage was that at no stage did it sound like a milkfloat and the engagement mechanism will not need adjusting in anyway as a result of other changes to the car. People have been DSQ’d for forgetting to adjust or failing to engage reverse when asked by the scrutineers.
First up I fitted the new drive chain, and then removed again once I realised I’d wrapped it around a chassis member! D’Oh! The second time around it was fine though and my new style tension blocks seems to work very well too. however looking at this picture I guess I could easily take 6″ out of the wheel base of the car or move the engine back by that amount..

So after a quick check of water, oil and fluid levels and a brief repair of a weepy hose that hadn’t been tightened properly during the engine refit last week we were off. 20ft up the drive and 20ft back again. 20ft up the drive and 20ft back again. Repeat until grin is firmly established :-)

Two or three things followed the test.

  1. The clutch is nicely progressive with lots of feel.
  2. The brake master pedal is a bit slow to return to it’s proper position and feels like it needs a clean and lube.
  3. The car seems reluctant to move. Getting out and pushing reveals a lot of rolling resistance.
  4. The exhaust will need extending and re bracketing. When you pull the diff rearwards to tension the chain the offside CV joint boot fouls on the exhaust.
  5. Engagement of forward and reverse is a bit stiff and could probably do with a lever to control it rather than the current T bar.

Of these the rolling resistance was of most concern . Was the diff a bit stiff or was it new brakes binding? I removed the pads and retested and she moved nice and easily so it was the brakes. However this did set me thinking about the Diff and how I needed to change the oil. So I emptied it out and it had a pretty nasty metallic sheen with a fair few particles of aluminium in it. Plus the magnetic sump plug had a nice furry coat of steel particles. I mentioned this to Graham at Nova and offered to strip the Diff down and inspect it. I’m not sure that I’ve got time for this before Brands and I don’t want to miss another meeting. So a flushout with petrol and new oil will have to do until then. On reflection the steel fillings are probably from the dog teeth which engage reverse or forwards and inexpert handling could easily have had the grinding a bit.

Still something to worry about a bit later.

However, armed with a rush of enthusiasm I’ve set about the long list of odds and sods jobs that weren’t on the critical path to movement but which must be done before we are going to the track. These included.

  1. A whole bunch of wiring and electrical work, tiding and binding up looms, running a 12v feed to the DL1 for Palm dash’s laptimer, fitting 6.7R resisters (actually 10x67R in parallel) to defeat the HESD linear solenoid.
  2. Removing the Lambda sensor dial and cabling as Tony Law forgot to fit a mounting boss for it,
  3. Running a control line to the bodywork connector so I can have an high mounted oil pressure warning light in my line of sight.
  4. Tidying up on side of the car to such and extent that I can actually fit the side pod.

The last job of the day was to commence fitting the external injectors and inlet pipes to the airbox. This is a bit more difficult than it looks as the floor of the airbox must sit nicely on the engine, and the top must of course line up with the bodywork. Still I’d done most of the preparatory work previously and pretty much all that was left was to glue and rivet it all in place.

Work on the airbox also included replacing a perfectly good and previously MSA approved rain light with a new one which must now be FIA instead of MSA approved. Out goes a £7 quid unit and in comes a new unit that should have cost upwards of 40 except I got it off ebay. Bah! this just seems to be a way of adding more cost.

Still a pretty successful day all round and I seem to be running out of excuses not to be at Brands Hatch on the 19/20 of May :-)

Posted in Diff, Reverse | Leave a comment

Gear linkage and Drive chain Numptyness

Last night I remade the gearlinkage by shortening the lever and returning the pivot to its previous position. The need to add an intermediate bell crank to the gear linkage in order to drive the high mounted actuation lever on the box has meant that the lever ratios and travel have changed.

The upshot of this is that with lever had a very small “throw” but required a lot of effort to move it (force and distance being proportional in levers). Now I’m not small or puny (Dan once said that watching Tim and me both exert maximum effort on the same recalcitrant part was amongst the most scary things he’d ever seen) but not being able to change gear without an audible grunt of effort seems a bad thing.

So I shortened the bottom of the lever and returned it to the original pivot position which had the effect of doubling the lever ratio. Now I still have a nice short throw on the lever but one that doesn’t require enough effort to make my temple throb when changing gear.

So with driveshafts, brakes, gears, exhaust, fuel and coolant the last thing to put in place before this race car moves again is the drive chain. I’d ordered a new one up from B&C express. But my personal numptyness quotient kicked in and it’s a tad too short as can be seen from my entry to the “Most inappropriate use of heatshrink in a structural role” shows.
Currently I’m waiting for another one and once that’s here to quote the automotive loon Murray Walker it’ll be “Go Go GO”
Posted in Uncategorized | Leave a comment

Its running again and getting close to moving

A fair amount of progress has been made this weekend. First up Duncan and I refitted the engine following fitting the baffle plate last week. This took a leisurely three hours. Before fitting the engine I took fellow racer Gordon Griffin’s advice and eschewed the exhaust heat wrap as nasty horrible & ineffective. In order to protect the fuel tank and my arse on the other side of the bulkhead I stuck some heat reflective blanket on the engine bay bulkhead. With the engine bay empty I also painted up a a few areas where I’d welded brackets in place and tidied up the wiring an main earth points.

By Lunchtime we were ready to fill the coolant system and restart the engine. With the engine idling nicely we then kept adding oil until the running level at idle was on the Max mark in the sight glass. This took 4Litres in all ( with a new filter) and I now need to understand how much over fill is required beyond this point I’ll be asking Andy Bates next week.

With the engine and drive line in place I was ready to move on to the brakes. My ultimate aim was to get the brakes sorted out, fit the drive chain and then have the beast move under it’s own steam up and down the drive.

First up was the brakes. The trial fit of the calipers yesterday proved that they would fit under the wheels so I set about permanently fitting them up. However we did hit a problem. The Calipers are made of four major parts, the two halves are separated by a pair of aluminium spacers. In my case the spacers in both calipers were oversize and actually prevented me from fitting the pads. So it was time to disassemble the callipers remove the spacers and set about them with a file. so after a couple of hours of fettling I actually had calipers that fitted on the car AND to which i could fit brake pads. Then I set about fitting the brake lines and doing a first bleed of the brakes system. Unfortunately this revealed a leaking front master cylinder which took a bit of rectifying and burnt through the reaming time in the day. Still the engine is running and I have a largely complete braking system. Although another slight wrinkle is that the mintex 1144 pads are a bit too thick to fit when new.

Posted in handbrake calliper | Leave a comment